So Anya and I had our windlass design essentially finalized. We started by constructing a cardboard model to test how pieces would fit together. Everything looked good and we got the design approved to we moved on to drawing out our designs on SolidWorks.
After finishing all the pieces and assembling them, we had it checked by the professors. We realized (we their help) that the washers that we had hoped would fit snuggly would probably fall out. We designed a couple versions of these exterior 'washers' that would keep the rotating interior piece from falling out. At first it was a larger circle to cover the inner one, but then we made a C-clip shaped one to save material (also it was easier to piano wire later). We also added the hole and 2 little prongs on each side of the spool to guide the string.
Evolution of the Spool
Here we widened the spool after realizing it wouldn't be able
to span the table with hthese
These are the pieces that were heavily reliant on the thickness of the delrin (4.970 mm). The tight fit is what would have held them together
Interior Washer
We ended up keeping the notch part that would be cut out as scrap from the delrin as a
plug to keep the spool in place.
All our original pieces
Attempting to fit in the clip
Finally we were ready to print. We sent and out pieces to the laser print, printed them, and assembled. We noticed that the pieces were not fitting properly the base was wobbly and didn't fit properly with the other pieces. We check the delrin and realized that it our pieces were printed on the wrong thickness. We realized that part of this problem was also that the notches were long enough and that was part of the wobbling- the top part of the base could not reach the table. In order to conserve material, we adjusted the length of the notch on only the bottom base piece. We reprinted the parts that we need- some parts such as the base took into account the thickness but other such as the spool were independent of the thickness of the delrin. We put the Windlass together (without fastenings to make sure everything fit. At this point we wrapped of the day but returned later to finish. All we really had to do was piano wire the clips to each other through the washer. (Ideally this would have been a magical tight fit but the laser cutter melts a certain amount of the plastic and we would have to experiment with sizing and such.)
And the we were finished! We tested it out and it worked! Anya took a video on her phone as proof that it worked. We were a little worried about the spool- it started to bend a tiny bit, and then more and more after each test so we left it alone. In our original plan we did say we wanted to double layer the spool, but we saw it as unnecessary at this point and it would have wasted material. Another problem was that the spool moves in and out so the handle sometimes hits the base piece. We did think about this happening and tried to avoid it but I guess our calculations weren't perfect. The other change I would have made was to add a horizontal base. Our windlass has essentially 3 major components that move independently from each other, so it wobbled a lot as we cranked it. I would have connected the to base pieces in some way that would keep them grounded but not get in the way of the bottle.
In the end our windlass worked and I am very happy with out design!